I bought my first Little Green Machine in 1994. It was a first-generation, ugly, dark green box with one purpose: to suck up pet accidents and spills. It was the only thing on the market at that time, and I desperately needed something to assist in cleaning up after an aging dog with bladder control issues. It worked well, and I got several years’ use out of it for my $70.00 investment. Eventually a plastic hose barb cracked inside the unit and I couldn’t find a replacement so I trashed it. Bissell has always had a policy of refusing to supply internal repair parts to customers, thanks to paranoia about consumer lawsuits.
I purchased a newly redesigned model at that time—one that sort-of resembled an egg standing on its fat end. It was a poor redesign with some flaws (like solution heaters that constantly failed) that I made do with for several years. I must say here that Bissell was good about support. After writing to complain twice about product failures, they replaced the unit both times at no charge. The second exchange was for the first version of their 1400-series model (Figure 1) , which at the time was brand-new.
I’ve been through three of these in the last six years. After the first unit of the new series died, I began studying their design to see how I could service it myself (and extend its life a few years as well). These things have gotten progressively more expensive, and my last replacement was priced just over $100.00. For that amount of money I expect something to last longer than a year!
Quirks and Design Flaws
The first redesigned 1400-series model had a simple storage clip on its backside that you’d snap the hose’s sprayer wand into. The wand was always popping out of the clip and hitting the floor, which would eventually crack the sprayer head and further decrease its already weak suction. Other problems included: the solution heater would die, the sprayer would simply stop working, or would begin to clog after using the unit for six months or so. The wand would drip cleaning solution after you finished using the unit and were putting the wand away. Finally, the cleaner would develop a stench from the urine I’d be cleaning despite rinsing the unit‘s recovery tank after each use. This is due to the way the recovery tank is designed.
You can see by looking at Figure 2 that there are a couple of problem areas (circled in red) near the recovery tank’s top. These seem to collect material that eventually begins to smell. Simply swishing hot water around in the tank is not sufficient to clean the areas, and you cannot access the tank’s insides to physically wipe the surfaces clean. The sprayer head and wand connection point was designed such that dirty water tends to collect in the nooks and crannies which also creates an unsightly, stinky mess. This junction also provides a break in the air stream and contributes to the unit’s biggest problem– it simply doesn’t have much suction power. The area you clean will remain fairly damp.
Design Improvements in newer models
I kept that original 1400-series model going for three years, by my estimates about two times longer than I should’ve been able to. The fixes were fairly simple for a geek to do. The recovery tank sat on a very thin rubber gasket that was glued to the main unit’s base. This was in addition to the rubber gasket on the tank itself. The base unit’s gasket began to wear away after a time, and I managed to make a replacement from some sheet rubber I purchased off of eBay. I cracked the sprayer head attachment apart and re-glued the pieces together with five-minute epoxy. I also glopped extra epoxy into the designed-in gaps and cracks while I was at it, which helped increase suction. I finally had to retire the unit after trying to discover why its motor was whining so loudly. After I took the unit apart to possibly oil the motor I learned more about the unit’s Achilles’ heel.
The currently-sold unit has several design revisions that seem to address some of the problems. The wand clip on the unit’s back has been redesigned and includes a swivel arm that locks the wand in place. Hallelujah! No more dropped sprayer wands! The sprayer hose has been changed from a solid green to a greenish-tinted clear hose. This allows the user to see how much crap is in the hose (and tell how well the suction is working). The recovery tank’s base gasket is gone (shown in Figure 3 sans gasket), which also eliminated a source of fluid leakage into the base.
Finally, Bissell redesigned the sprayer head with better welds and eliminated the extra gaps. This helps to a degree, but the redesign introduced several new ways for dirty solution to collect in the sprayer/wand connection and stink up the works. They did nothing to redesign the collection tank tower, which still collects material that leads to ‘Stinky Tank syndrome.’ My current unit had its hose replaced twice, once under warranty. (This may have been due to my sucking up hot water in order to flush and de-stink the unit.) The original hose was a little too short and it was under stress when the wand was placed into the clip. The stress also ended up breaking the clip after the unit was no longer under warranty. I performed a couple of simple fixes to increase its suction but didn’t implement anything major. I performed the second hose replacement myself, as I finally found a source for internal parts. I had to buy a second unit while waiting for the parts to arrive as they were backordered for a month-and-a-half.
Why doesn’t it suck (enough)?
The Bissell Little Green’s designers had a challenge, I’m sure…how could they suck up a spill and easily separate the water from the air? Most wet/dry vacs have a foam filter that the suctioned air passes through, which keeps the water out of the exhaust. I’m sure the designers didn’t want their customers to deal with replacing a filter (liability lawsuits, you know!), given the tendency for most consumers to screw up the simplest of operations. This probably led to the current design.
Suction is provided by a motor with a squirrel cage fan attachment located in the base. Air and water are pulled into the sprayer head, through the hose and into the recovery tank. The tower-like structure you saw in Figure 2 is divided in half. The water falls into the tank since it’s heavier than the air, and the air exits the hole in the opposite side of the tower. The air stream then passes the fan/motor assembly and is blown out the unit’s backside. Simple design, yes, but flawed. The air has a high degree of moisture in it, and there is no filter of any kind to protect the metal motor and blade assembly. If you have too much suction the air will have even more water in it; this will accelerate the disintegration of the motor and allow water to blow out of the exhaust port with the air. You read that right—the motor will disintegrate faster. This is the Achilles’ heel I mentioned earlier. When I disassembled my last unit to try and oil the motor, I discovered that the blades and motor casing were so rusty that they practically fell apart in my hands. That was what caused the motor to scream and whine. This is a marketing textbook example of built-in obsolescence! At the time I didn’t know where I could get repair parts, but now I know and will share the source with you.
Making Things Suck More
So, we know that the unit will eventually stop working due to the disintegration of the motor. Should that stop us from making the unit work a bit better? NO! If it’s going to have a finite life before we have to repair it, let’s mod it to perform its job better.
Look at the sprayer/wand connection in Figure 4. You can see a rubber O ring that attempts to seal the wand/sprayer connection point. In my last unit this O ring was so loose that no seal was taking place. I went to the hardware store with the old ring and found a new one that was a little thicker. Its size is given as a “number 32.” I replaced this ring, which now requires the user to jockey around a bit when removing/reattaching the sprayer head. The improvement is well worth the additional effort that will be required.
Now take a close look at the sprayer head/wand. If you’ll notice, there’s a button that you have to press down on to remove the sprayer. This is located on a molded plastic lever that flexes when the button is depressed. This design feature also allows a good deal of suction to exit the hole around the lever. Additionally, the end of the wand does not seal inside the sprayer head. This is a second point that allows air to exit around the lever and allows dirty water to accumulate. Sealing that leak will require a bit more work; however, we can significantly increase the suction by installing a flat rubber seal into the wand below the button/lever assembly. How much additional suction does that give? I don’t have a scientific method to gauge it, but by simply holding the sprayer head against my hand with the unit running before and after the mod, it feels as if I’ve approximately doubled the suction.
I took a piece of 1/16” thick sheet rubber and cut a 1.5-inch by 3.5-inch piece from it. I then applied rubber cement around the edges of the piece (Figure 5) leaving the center dry.
This is important! If the rubber adheres to the lever, it will be extremely difficult to work the lever and remove the sprayer head. Next, I folded a piece of paper from a magazine (Figure 6) and inserted it into the slot around the lever.
This allows you to apply contact cement around the lever without accidentally getting glue on the lever itself. Apply rubber cement to the inside of the wand in approximately the same area where the rubber will go as in Figure 7.
After applying the cement into the wand, quickly pull the paper out of the slot. Now wait about five minutes to allow the glue to get tacky. After you’ve waited, flex the rubber piece in an arc as shown in Figure 8 and carefully insert it into the end of the wand with the glue side facing the glue inside the wand. DO NOT ALLOW THE PIECE TO CONTACT THE GLUE INSIDE THE WAND UNTIL IT’S IN POSITION. If you do, it will be extremely difficult to remove. You may want to use forceps or tweezers to assist you in alignment.
Once it’s aligned, press the rubber into place, exerting pressure around the edges of the rubber. You may have to use a tool to reach in and push the edges down.
Let the piece sit overnight to dry; then reattach the sprayer head and turn the unit on. You can hear a little bit of air still exiting the hole around the button. Hold the sprayer against one hand and cover that hole with your opposite thumb. If you tried the suction before the mod, you should notice a considerable difference in the amount of suction after the mod. If you wish to cover the hole with a piece of electrical tape you can easily seal the leak, and remove the tape when you wish to clean the unit. Alternatively, simply cover the hole with your thumb as I do while using the Little Green. I am considering milling a second channel around the end of the wand with my Dremel tool, then using a second O-ring to completely seal the connection. This would allow for more comfortable use of the sprayer wand.
Some tips on using the Green Machine
1) Clean the unit after each use by holding the sprayer head under warm (not hot! I learned my lesson…) running water. I will sometimes mix some pine-scented cleaner with water in a bucket and pull that through the hose. Note that you can only suck so much fluid into the recovery tank; there’s a white line on the tank showing the maximum level. When you’ve finished flushing the sprayer head and hose in this manner, hold the sprayer head above the unit pointing upward for a moment or two to allow all the remaining water in the hose to be sucked into the recovery tank.
2) Stopping the dribbles. When you’ve finished cleaning a spot and you’ve turned the power off, hold the sprayer head above the unit pointing upward and depress the trigger. Hold the trigger in for a count of five before releasing it. MAKE SURE THE POWER IS OFF BEFORE DOING THIS OR YOU’LL SPRAY HOT CLEANING SOLUTION ON YOURSELF OR SOMEONE ELSE. Performing this maneuver allows any cleaning fluid still in the hose/sprayer head to drain back into the unit, and prevents leakage when you’re moving the sprayer head around to clip it onto the unit.
3) Clean the recovery tank after each use. Do not allow material to stay in the recovery tank! This allows the material to soil the plastic and contributes to ‘Stinky Tank syndrome.’ Dump the recovered material into the toilet and flush it. Use the toilet because any pet hair in the water may clog your sink drain. Run hot water into the tank from the top hole, then turn and twist the tank to thoroughly swish the water around before emptying the tank again into the toilet. Remove the rubber gasket from the bottom of the tank and clean it with soap and water or pine-scented cleaner as well. Material tends to collect on the backside of that gasket and also creates a smell. If you have a bucket that’s big enough, you can dump the entire tank into a water/pine cleaner mix and get things smelling a bit better.
4) Use only distilled water in the unit. I cannot stress this enough. The minerals in tap water can build up after awhile and collect in the heater assembly. This can clog the sprayer when bits of the accumulated minerals fracture off and mix with the cleaning solution. When the sprayer wand gets clogged you’ll see that fluid has entered the head but nothing exits when you press the trigger. To remove the clog you can usually insert a cotton swab into the channel inside the sprayer head, and gently move it around to catch and remove the clog. Occasionally the clog gets wedged into the sprayer hole; this requires pushing a slightly-bent straight pin into the hole from the outside to push the clog out. You can then use the cotton swab to remove it.
The heater itself can be cleaned by first disassembling the unit and then removing the cover on the heater but it’s a major hassle. The heater box sits atop some plumbing bits and has a thin hose entering and exiting on its sides. To get inside it you remove the screws that hold the top cover on. You’ll see maze-like channels inside the heater, and should see whitish material inside those channels. Those are the mineral deposits, and you remove them by scraping them out. You’ll then replace the top cover and reassemble the base. This can take up to an hour the first time you do it.
Getting Repair Parts
I don’t know why it took so long for me to find a parts dealer (despite Google), but Hesco Sales (www.hescoinc.com) will sell you any part they can get from Bissell. There’s a section on their website where you enter your unit’s model number and can pull up exploded diagrams of the unit to help identify your part. In my case the part data wasn’t available on their site. Several emails later they had the part information and made the part orderable. Note that they have a $25.00 minimum order, so my advice is to get a couple of the hose clips I mentioned earlier. They’re inexpensive and make good filler material for your order. Besides, you’ll eventually need them.
Hopefully you found this information useful, and maybe you will be able to save your unit from the trash heap (or have gotten the courage to rescue one from the thrift store). If one person can keep their unit running longer I’ve done my job.
20 responses to “Hacking / Modding the Bissell Little Green Cleaner”
You’re my kind of obsessive. Thanks for your help. Do you know if the wand sprayer comes apart or if it is glued together?
Matt, the sprayer’s glued together. That’s a piece you’d have to write off and get a new one.
This is a huge help. One technical question. The collection tank gasket has 2 sides, one of which is open and the other which tapers into a narrow sleeve, presumably to prevent back flow. Which side of the gasket should be placed into the higher recovery tank tower? I cant figure it out logically, and we are needing the little green machine more because our dog is reluctant to go out when it is below 0.
Tom, if you’re holding the tank with the flat side up and looking at the gasket end, the big tapered end will go on the bottom. It’s nearly impossible to put it in backwards as there is a notch on one edge of the gasket’s flange that fits around a stub that’s nearest the flat side of the tank.
thanks so much!
Hi vvenesect, I am amazed at this article. This looks like something I would think about doing but never actually giving enough effort to post. So, thank you very much for your follow through. Secondly, I am trying to replace the main suction tube, but could not disassemble the unit any further to reach the end of the small black tubing that is attached to the main tube. It is burried in the machine and I cant get any closer to it. Can you help?
Justin, from what I remember I had a difficult time of doing that myself. I believe I had to strip it way down in order to get to it. I have to replace the hose on one of my two machines again, so I’ll definitely take notes and pictures of the process for the blog.
Is it hard to replace the hose?
No, not if you take your time and watch where everything is connected. It’s just tedious as you have disconnect a number of things before you can get to where the hose connects.
Thankyou for all your diligence. I have been searching for the o ring in figure 4 as mine disintegrated after 2 – 15 minute uses then 2 yrs of pampered closet storage. Mine is a 1400D model, not heater but has the short see through hose and wand storage clip you mentioned.
I’m in Canada and would love to know where you found “number 32” o ring replacement. The thinnest O ring is still imperceptibley too thick to allow brush to fully pass and lock, even with alot of jockying around.
Bissell and local service agent informs me they dont sell just the o ring but instead I wouod have to buy the hard handle or likely the whole hose assembly to replace this 10 cent o ring. I’m Pissed!
I will use your flat rubber seal fix… brilliant…I will fill in other manufacture seams with apoxy as I inspect for suction leaks.
How though do you recommend solving moisture over fan etc in air venting? You mentioned a filter, like the hole filled sponge kind in wet vacs. Is it worth dremelling a “door” access to this area, hinge it, put liquid rubber gasket around edges for air sealing if needed to replace material dremelled away… all to access this area and insert a sponge filter between air venting line and fan/ motor. In this way a person could pop open the door, pull out sponge to dry before next use, saving motor fan from rusting?
I never opened mine up to see if cutting an access in plastic body would even gain access to this area you mentioned easily.
But if you think its plausible, would you mind trying something out and posting it back here with the how to’s?
Thanks again… dont know why Bissell juat doesnt hire you in research and developement. I live in a travelling RV community. We meet litterally hundreds of other RV ers all over the continent. They in turn each meet hundreds more…and so on and so on.
when I pulled out my Bissell, 5 women gathered around very interested in purchasing one…until of course the O ring issue and no parts, service or help available.
I told Bissel this, that they could have had many units sold asap and through word of mouth, thousands more. But instead they lost all that business over a 10 cent piece.
I bet thier stock holders would be pissed to know this. The actual customers and potential customers already are.
Kay in Canada
I purchased my O ring at a local Ace Hardware store. It was located with the plumbing supplies in a set of plastic bins that had all sorts of gaskets and O rings. If you have Ace Hardware in Canada I’m sure you can find them. As for a solution for keeping moisture from destroying the motor…I’m afraid there’s nothing to be done. It’s due to the way the unit was originally designed and there isn’t a way to work around it. Perhaps fabricating the motor and blower cage of a rust-resistant material would help.
Hi Vvenesect – I love this article. Thanks for sharing your analysis and repair/improvement strategies!
I love figuring out how things work and most of my friends and family think my curiosity is odd and my determination to fix things is silly (until I fix their thing and then they love it :). I also just hate throwing things away (even when I’ll get a free replacement). It seems such a waste of all the functioning parts of a machine to let the small defects doom it to the trash…
I just had mine start leaking (or at least this is the first I’ve noticed) from the bottom. Took it apart, cleaned up seals etc. One curious thing I noticed – a small round hole in the middle of the bottom panel (in the centre of the round “sealed” section)… Have you seen this in yours? Very odd – it goes straight through… Any moisture that gets into that section would surely drip out. It clearly wasn’t the source of the leaking I saw because that was coming out of the very edge of the bottom panel (which means it must have escaped the seal or had some other internal leak that made its way through). Anyway, plugged that little hole with hot glue and with cleaned seals etc. no evidence of leaking anymore.
It’s nice to know there are kindred spirits out there who see the satisfaction in analyzing, fixing and/or improving things. And very interesting tip re the distilled water… Thanks again!
I have the exact one and the sprayer head cracked and broke and i found a new one online for $6.99 and now it works like it is new again.I do have a problem trying to get the dirty tank clean i can never get to all the grime off of the plastic edges.This machine works better then my big steam cleaner it is a must have if you have pets.
What an excellent article! I too fix everything I can get my hands on. I’ve had my LGCM for years now, and I always rinse the tank, and make it suck up warm water after each use. By the way, Bissel needs to hire you immediately! 🙂
I recently repaired my little green. mine is one of the originals. I paid $50US for it back in around 2004. I was surprised at how much they have gone up in price. I had to replace the inner base gasket and the waste container gasket. both had deteriorated, especially the waste gasket. I bought a piece of 0.5mm silicone rubber with a 3M adhesive back from ebay and cut new gaskets. The hard part was repairing the brush handle – the channel hat connects to the water nipple on the hose end was all cracked and leaking. I cut away the broken parts leaving about 1cm of channel ahead of the outlet hole. Then I designed a replacement coupler to connect the nipple to the remaining channel. I printed the part on my 3D printer and it works with a nice tight fit, no glue. it leaks a tiny bit. i will put a small amount of CA glue around that to seal it up.
Here’s a link to a picture: http://usabilitynow.ca/pictures/IMG_8577.JPG
Once again, 3D printers save the day. 🙂 I need to get one of those.
wow great info, I can’t believe I haven’t found you sooner. If anybody is still following this thread, I am still trying to figure out how to clean the recovery tank, specifically the parts that accumulate the stinky bits, the parts you circled in red in the first pic. any suggestions out there?
I submerge mine in a tub filled with warm-hot water and Pine-Sol cleaner mixed in. Make sure the water fills the tank, let it sit for a while, then dump it out and repeat with the tank’s opposite side facing up. Repeat, then flush with clean water and let dry. You’ll never get it all out but it helps.
Hi there, Thanks for sharing your in-depth awesome geeky tinkering.
I’ve got a little mystery on my hands and I suspect you may be able to help.
My little green proheat is leaking from the bottom. I have disassembled it to check for any broken parts, leaks etc. Everything looks good, except I may have a missing gasket and I believe you discussed this part in your write up, but I have a question to clarify:
You wrote: ‘The recovery tank sat on a very thin rubber gasket that was glued to the main unit’s base. This was in addition to the rubber gasket on the tank itself. The base unit’s gasket began to wear away after a time, and I managed to make a replacement from some sheet rubber I purchased off of eBay.’
It appears in your photo (figure 3) There is no gasket visible on the units main base. Is that a picture of the base before you installed your diy replacement gasket? (In other words the gasket that should be there is not visible in that photo?)
I think i’ts possible the reason my unit is leaking is because the base gasket for the recovery tank some how came loose and is MIA without my knowledge. As my base under the recovery tank looks exactly like the photo your posted in fig 3. There is just white pastic there, no black gasket.
Is this the part you made on your own out of sheet rubber to replace? https://www.ereplacementparts.com/gasket-for-baserecovery-tank-p-762996.html
As it appears there are no longer replacement parts available, I may have to make my own, but I want to make sure there is indeed supposed to be a black gasket there, before I go through the trouble to make my own.
I’ve been looking at part diagrams and the base / recovery tank gasket is not shown on diagrams but is only mentioned in *miscellaneous parts.
Thanks for reading my post!
Hi Karen, and thanks for your questions.
The part you referenced is the part that was once needed between the tank and base. As you noticed in my pictures the gasket was not present. It was apparently required in early models but was no longer necessary when I replaced my original unit. However, that isn’t the part that would cause your present issue.
There is a gasket between the upper body and lower plate shown under callout #34 on this webpage: https://www.ereplacementparts.com/bissell-1400-little-green-machine-parts-c-129994_377487_346027.html . It’s called a “Bottom Base Cover with Gasket,” part number B-603-5031. This seal has failed. You could buy some 1/32″-thick sheet rubber from a local supplier or eBay seller and try making your own. You’d pull your old gasket and lay it on a piece of paper or very thin cardstock, making sure you arrange it so the semi-circular part is round and the rectangular part is correctly oriented, then trace it with a pencil for both the inside and outside edges. Use that as a cutting template on the rubber. You’d need an X-acto knife with a fresh sharp blade and a steady hand. I’d cut the inner part of the template first, then trace the hole onto the rubber with a fine-point Sharpie. Next you’d cut out the outer gasket edge on the paper and use that to trace the outer edge onto the rubber.
You could also try using “rubber rejuvenator,” which used to be available at RadioShack for cleaning tape machine rollers and belts, and might be available at shops that still repair typewriters as a “platen cleaner.” If you do this make sure you clean the channel in the base where the seal resides, as well as the part of the upper base that rests on the gasket, using something like window cleaner before resealing the unit.
Good luck with your repair! You made me look back on this issue and realize that a further failure of my remaining unit will mean I’ll have to buy a newer model…